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Transocean Investigation Key
Findings This summarizes the key findings of the
investigation team based on its extensive review of available
information
concerning the Macondo well incident.
As operator of the Macondo well, BP directed all aspects of its
development. It chose the drilling location,
designed the drilling program that included all operational
procedures, set the target well depth, and created the
temporary abandonment procedure for securing the well before
departure of the drilling rig.
As drilling depths increased at Macondo, the window for safe
drilling between the fracture gradient and the
pore-pressure gradient became increasingly narrow. Maintaining the
appropriate equivalent circulating density
(ECD) became difficult, and BP experienced several kicks and losses
of fluid to the formation. BP’s knowledge
of the narrowing window for safe operations guided key decisions
during the final stage of operations.
BP’s changes from the original well plan in the final phase
included:
• Reducing the target depth of the well
• Considering changes to the well casing
• Using a lower circulating rate than the parameters specified to
convert the float collar
• Reducing cement density with nitrogen foam
• Using a lesser quantity of cement than that specified in BP
procedures
• Deciding not to perform a complete bottoms-up circulation before
cementing
Although aimed at protecting the formation and allowing operations
to continue toward completion of the well,
these decisions set the stage for the well control incident.
Running Production
Casing BP chose a long-string production casing
design that required the development of a minimal and
technically complex cement program to avoid damaging the formation
during cementing, leaving little
margin for error within normal field accuracy. BP and Halliburton
then increased the risk by failing to
adequately test the cement program.
The investigation confirmed that the operator’s long-string casing
design met the loading conditions that were
experienced prior to and during the well-control incident. The use
of this design, however, drove other plan
departures that ultimately increased risk and contributed to the
incident. Primarily, cementing the casing required
a complex, small-volume, foamed cement program to prevent
over-pressuring the formation. The plan allowed
little room for normal field margin of error; it required exact
calculation of annular volume and precise execution
in order to produce an effective barrier to the reservoirs.
The operator had other abandonment alternatives. BP could have
either installed a liner and tie-back or
deferred the casing installation until the future completion
operations began. Either approach would have
placed additional and/or different barriers in the well prior to
the negative pressure test and displacement.A
Deferring installation until future completion operations would
have allowed additional time for detailed planning
and verification of the design.
Converting the Float Collar BP deviated
significantly from its plan to convert the float collar, but
proceeded despite observations
of anomalies. The investigation team found it possible that the
float collar did not convert and thus left
a clear path for hydrocarbons to flow from the formations to the
rig.
BP’s planned procedure to convert the float collar called for
slowly increasing fluid circulation rates to 5–8 barrels
per minute (bpm) and to generate pressure of 500–700 psi at the
float, consistent with the float manufacturer’s
guidelines. However, because of the increasingly narrow window to
avoid fracturing the formation, BP deviated
from its planned conversion procedure.
BP made nine attempts to convert the float collar over the course
of two hours. BP never circulated at a rate
of more than 2 bpm, but it did increase the pressure applied on
each successive attempt, finally achieving
circulation at a pressure of 3,142 psi — almost five times that
planned — and a flow rate of 1 bpm, less than ¼
of that planned. BP took this result as an indication that the
float collar had converted even though the resulting
circulating pressure was lower than BP’s model had predicted. The
BP well site leader expressed concern about
the issue, took steps to investigate it, and discussed the question
of whether the float collar had converted with
the Halliburton cementing engineer and BP’s shore team. Halliburton
and BP proceeded, apparently having
concluded that the float collar had converted.
The investigation team found it likely that debris in the wellbore
may have plugged the shoe-track assembly
and float collar and blocked circulation during the first eight
attempts to convert the float collar. The increase to
3,142 psi may have cleared debris from the system without
converting the float collar. If the float collar failed to
convert, the cement program may have been further compromised.
Cementing The precipitating cause of the
Macondo incident was the failure of the cement in the shoe track
and
across the producing formations. This failed barrier allowed
hydrocarbons to flow into the well.
The cement failed as a result of a number of factors that stemmed
from BP’s ECD-driven management decisions
between April 12 and 20, 2010. These factors include the complexity
of the cement program; inadequate testing
of the cement; likely cement contamination during the operation;
and inadequate testing of the cement after it
had been pumped.
Complexity of Cement Job BP required a cement program
that would exert minimal pressure on the formations. To minimize
pressure,
Halliburton devised a plan that called for pumping a small volume
of cement, much of it nitrified, at a low rate.
While this plan would help BP avoid losing cement into the
formations, it required precise execution, left little
room for error, and increased the risk of cement contamination.
Cement Program Tests Despite the inherent risks of
cementing the long-string production casing in the conditions at
Macondo, BP did
not carry out a number of critical tests (e.g., fully testing
setting time and cement compatibility with drilling fluid)
before or after pumping the cement. Post-incident testing by both
CSI Technologies and Chevron demonstrated
that the nitrified cement slurry used at Macondo likely failed.
Cement Contamination Contrary to best practices, BP
decided not to perform full circulation — or a “bottoms-up” — to
condition the
drilling fluid in the well before the cement job. A full bottoms-up
circulation would have required approximately
2,750 barrels of clean mud to be pumped into the well over about
11.5 hours to keep the ECD under the
maximum limit. Instead, BP decided to circulate only 346 barrels to
reduce the chance of fracturing the
formation, increasing the likelihood that debris remained in the
wellbore after circulation.
The failure to run a full bottoms-up, coupled with the fact that
drilling mud in the well had not been circulated for
more than three days, suggests that cement in the annulus could
have channeled and become contaminated.
This could have delayed or prevented the cement from setting and
developing the required compressive
strength. Pre-job testing of the cement and spacer/mud/cement
compatibility was not sufficient to rule out
contamination.
Post-Cement Program Review Testing of the adequacy of
the cement program could have identified areas of concern, but was
not done. After
approving the cement program, BP proceeded with its temporary
abandonment plan.
Temporary Abandonment Procedure BP’s final
temporary abandonment plan contained unnecessary risks that were
not subjected to formal
risk analysis.
BP engineers generated at least five different temporary
abandonment plans for the Macondo well between April
12 and April 20, 2010. The plans varied considerably, as did the
level of risk they introduced. The abandonment
procedure ultimately implemented at Macondo never received the
required MMS approval. Further, it was
not developed and delivered to the Deepwater Horizon until the
morning of April 20, 2010, after the rig had
commenced temporary abandonment operations. The investigation team
found no evidence that BP personnel
on the rig or onshore subjected any of the successive temporary
abandonment plans or changes to a formal
risk assessment process.
The safest of the five versions (that dated April 14) provided that
the surface cement plug be set in mud rather
than seawater and that a negative pressure test be conducted before
the drilling mud was displaced with
seawater. The plan that was finally implemented lacked both of
these features.
The most significant deficiency in the final plan was the
cumulative lack of barriers to flow. The final plan
required displacing the drilling mud to a depth of 8,367 ft.
(approximately 3,300 ft. below the mudline), which
was much greater than the normal displacement depth of between zero
and 1,000 ft below the mudline. In
addition, the plan removed the mud before testing the cement
barrier with a negative pressure test and before
setting the surface cement plug. As a result, no secondary cement
barrier was in place during the negative
pressure test and displacement.
Displacement The initial displacement was
planned incorrectly, and the execution did not meet the objective
of
allowing for a valid negative pressure test.
The final temporary abandonment plan required displacing the casing
annulus below the annular blowout
preventer (BOP) with seawater to achieve the desired negative
pressure test conditions. However, post-incident
analysis determined that this objective was not achieved because of
calculation errors in the final displacement
procedure, lower pump efficiencies which may have been caused by
the unconventional spacer materials,
potential downhole losses, and the movement of spacer below the
closed annular. These factors resulted in a
large volume of spacer in the annulus during the negative pressure
test that went unidentified due to inadequate
fluid volume tracking and lack of procedures to identify the
appropriate pressure readings for a satisfactory
initial test configuration.
With heavy spacer in the annulus below the closed annular BOP, a
valid negative pressure test could not be
achieved by monitoring the kill line, which was the method BP
decided to use.
Negative Pressure Test The results of the
negative pressure test were misinterpreted. After the test, BP
decided to proceed with
the final displacement.
A negative pressure test is necessary to confirm that the cement
will block flow from the reservoir into the
well after mud is replaced with seawater. There is no established
industry standard or MMS procedure for
performing a negative pressure test, and procedures vary from well
to well. At Macondo, BP was responsible
for overseeing the test and determining if the test was
successful.
Post-incident analyses confirmed that the test failed. Anomalous
pressure observed on the drill pipe during the
test should have alerted all of those monitoring the well to the
fact that the cement barrier was not effective, that
pressure was being transmitted past the cement and float equipment,
and that the well was in communication
with the formations.
Central to the misinterpretation of the test results was BP’s
decision to monitor the kill line instead of the drill
pipe when conducting the test. Had the drill crew continued
monitoring flow from the drill pipe, as they had
been doing previously, those monitoring the well would have
detected flow indicating that the well was in
communication with the formation
Test and Final Displacement Post-incident
analysis indicated a change in flow path from the well during the
final displacement
masked influxes into the wellbore.
Following its approval of the negative pressure test, BP directed
the drill crew to proceed with displacing the
riser with seawater and, when the spacer was expected at the
surface, to stop operations for a sheen test.
Replacing the heavier drilling mud with lighter-weight seawater
during final displacement eliminated the
remaining hydrostatic barrier to flow, leaving the inadequate
cement barrier at the bottom of the well as the
primary barrier. According to post-incident calculations, the well
became underbalanced to one or more of the
exposed formations sometime between 8:38 p.m. and 8:52 p.m., but
there was no clear indication of an influx
at that time.
Just before the pumps were shut down for the sheen test, the trip
tank was dumped into the flowline to send
oil-based mud back to the mud pits. Based on post-incident
analysis, the resulting increase in flow from the trip
tank across the flow sensors masked an influx into the well.
More than one individual on the rig indicated the well was not
flowing when the mud pumps were shut down
for the sheen test. It is possible that no flow was seen because
the flow path had been changed to overboard
to dispose of the spacer before the visual confirmations.
Post-incident data analysis shows that hydrocarbons
flowed into the well during the sheen test, but the overboard
discharge may have masked the flow.
Although the compliance engineer concluded and reported that the
sheen test was successful, post-incident
analysis indicates that the spacer had not reached the surface at
the time the test was conducted. This report
gave the driller an erroneous confirmation that the displacement
was on track when, in fact, it was not.
Pump operations following the sheen test masked an underlying trend
of increasing pressure which resulted
from an influx into the well. It is not known what data the drill
crew was monitoring or why they did not detect
an anomaly until approximately 9:30 p.m. At that time, the drill
crew acted upon a differential pressure anomaly
between the kill line and drill pipe. Actions taken indicate
behaviors consistent with a belief that the well was
secure and a plug existed in the well. At 9:42 p.m., the pressure
trend provided a conventional influx indication
with a drop in pressure. At that time a flow check was completed on
the trip tank and well control action followed.
Sheen Activation of the BOP The BOP functioned
and closed but was overcome by well conditions.
The Deepwater Horizon BOP and electro-hydraulic/multiplex (MUX)
control system were fully operational at
the time of the incident, and the equipment functioned. The
equipment was maintained in accordance with
Transocean requirements, and all modifications that had been made
to the BOP either maintained or improved
the performance of the device. Minor leaks identified pre-incident
did not adversely affect the functionality of the
BOP for well control.
Upon detecting flow, the drill crew shut in the well by (1) closing
the upper annular BOP; (2) closing the diverter
packer and diverting the flow to the mud-gas separator; and, (3)
closing the upper and middle VBRs, which
initially sealed the well.
However, because of the high flow rate of hydrocarbons from the
well, the annular BOP element did not seal
and the concentrated flow eroded the drill pipe just above the
annular. The closing of the VBRs isolated the
annular space and temporarily stopped the influx, but increased
pressure inside the drill pipe until it ruptured atthe point of
erosion above the upper annular. The ruptured drill pipe allowed
hydrocarbons to again flow into the
riser. When the Deepwater Horizon lost power and drifted off
location, the drill pipe parted fully.
The explosions and fire disabled the communication link between the
BOP and the rig, preventing activation of
the BOP emergency disconnect system (EDS) from the toolpusher
control panel.
The automatic mode function (AMF) operated as designed to close the
blind shear rams following the explosion.
However, high pressure bowed the drill pipe partially outside of
the BSR shearing blades, trapping it between
the ram blocks and preventing the BSR’s from completely shearing
the pipe, fully closing, and sealing the well.
Muster and Evacuation All personnel who
survived the explosions made their own way or were assisted to the
forward lifeboat
muster station and successfully evacuated the rig. Despite the
obstacles and challenges, the muster
and evacuation plans and training facilitated the evacuation of all
115 survivors.
The Macondo incident created extremely challenging conditions for
everyone onboard. The explosions and fire
happened in the evening, when many off-tour crew were asleep or in
their cabins. The blast damage blocked
some normal muster points. Some crew were injured and could not
evacuate without assistance. It appears
that, under the stress of the emergency, four persons evacuated
independently rather than pursuant to the
procedure in which they were trained.
Despite these obstacles and challenges, the muster and evacuation
plans and training facilitated the evacuation
of all 115 survivors to the Damon B. Bankston supply vessel nearby.
One hundred people evacuated in the
forward lifeboats, seven evacuated in one of the forward life
rafts, and eight jumped from the forward end of the
rig into the ocean and were recovered by the Bankston fast rescue
craft (FRC). After the survivors reached the
Bankston, the 17 most seriously injured survivors were airlifted by
USCG helicopters to hospitals for treatment.
In addition to the heroic actions of many of the crew, assistance
from the crew of the Bankston was critical in
the evacuation and rescue effort.
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